Report

McKee-9A Well Completion Report.

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The McKee-9 well bore was abandoned by removing the 2-7/8in production tubing, pulling the 5 1/2 casing from 650m AH, and setting a 15.6ppg cement plug from 647 to 516 metres. The plug was drilled out to 600m and kick-off of McKee-9A was achieved at 602m on June 8th, 2000. McKee-9A targeted potentially bypassed oil in the overthrust McKee Formation and intersected 93m of McKee Sandstone, before reaching a total depth of 2280m AHBKB, eight metres into the overthrust Mangahewa Formation. Wireline log interpretation indicated a net play of 92m, with 14m of gas, 63m oil bearing and 15m of probably water bearing formation. The well was completed as a production well. Also included are FCET Report 1066: Safety Plan during drilling and FCET: 1060 Drilling Programme.

Report ID pr2514
Class Petroleum
Type Well Report - Completion
Permit 38086
Operator FLETCHER CHALLENGE ENERGY TARANAKI
Commodity Petroleum
Region Taranaki Basin
Start Date 01 January 2000
End Date 31 December 2000
Report extents in GeoJSON
Author Murray D.
Data Format
  • PDF
  • TIF