This report discusses production testing carried out on the Stratford-1 well between November 1983 and January 1984. Stratford-1 produced a maximum of 3100 MSCF/D gas and 146 b/d condensate from the McKee Formation, which test analysis confirmed to have extremely low permeability in this well. Analysis of the production test pressure data indicated severe formation damage. Production rates were seen to increase during the long term flow period, and it was recommended that the well be flowed for a longer period to allow it to clean up and allow the true production potential to be assessed.